Simulation Study of an Automatic Trim System for Reducing the Control Forces on a Light Twin After an Engine Failure

850913

4/1/1985

Authors
Abstract
Content
An automatic trim system for reducing the control forces after an engine failure on a light twin has been investigated on the Langley General Aviation Simulator. The system schedules open-loop trim tab deflections as a function of differential propeller slipstream dynamic pressure and freestream dynamic pressure. The system is described and the airplane-system static and dynamic characteristics are documented. Three NASA research pilots evaluated the effectiveness of the system for takeoff and landing maneuvers. A variety of off-nominal system characteristics were studied. The system was judged to be generally beneficial, providing a 2 to 3 point improvement in pilot rating for the tasks used in the evaluations.
Meta TagsDetails
Pages
16
Citation
Stewart, E. and Brown, P., "Simulation Study of an Automatic Trim System for Reducing the Control Forces on a Light Twin After an Engine Failure," General Aviation Aircraft Meeting and Exposition, Wichita, Kansas, United States, April 16, 1985, .
Additional Details
Publisher
Published
4/1/1985
Product Code
850913
Content Type
Technical Paper
Language
English