Simulation Study of an Automatic Trim System for Reducing the Control Forces on a Light Twin After an Engine Failure

850913

04/01/1985

Authors Abstract
Content
An automatic trim system for reducing the control forces after an engine failure on a light twin has been investigated on the Langley General Aviation Simulator. The system schedules open-loop trim tab deflections as a function of differential propeller slipstream dynamic pressure and freestream dynamic pressure. The system is described and the airplane-system static and dynamic characteristics are documented. Three NASA research pilots evaluated the effectiveness of the system for takeoff and landing maneuvers. A variety of off-nominal system characteristics were studied. The system was judged to be generally beneficial, providing a 2 to 3 point improvement in pilot rating for the tasks used in the evaluations.
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DOI
https://doi.org/10.4271/850913
Pages
16
Citation
Stewart, E., and Brown, P., "Simulation Study of an Automatic Trim System for Reducing the Control Forces on a Light Twin After an Engine Failure," SAE Technical Paper 850913, 1985, https://doi.org/10.4271/850913.
Additional Details
Publisher
Published
Apr 1, 1985
Product Code
850913
Content Type
Technical Paper
Language
English